Current production is approximately 3,500 barrels of oil equivalent per day
(boe/d). The company said that production was negatively impacted by 500boe/d when the Triassic zone in the newly drilled 4-33 well at George unexpectedly encountered water production problems.

A remedial workover was performed in the last week but it was unable to recover gas production from the well. The zone is expected to be recompleted in an adjacent wellbore after break-up. The 4-33 well continues to produce 100boe/d out of the Kiskatinaw and has two additional uphole zones awaiting future completion.

Sabretooth has completed two Kiskatinaw wells drilled in December 2007 resulting in two gas wells. Both wells are expected to be on production by mid February 2008. One well encountered three pay horizons in the Kiskatinaw, British Columbia, Canada.

While the first well tested at 4.5 million cubic feet per day, the other two zones remained behind pipe for future recompletion. A third well in the area is expected to spud with multizone potential.